Author
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Topic: stumbling on acceleration
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skips69 Gearhead Posts: 124 From: Catlin, IL USA Registered: Mar 2001
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posted 05-25-2002 08:01 PM
Just curious before I throw parts and money at this problem: I have a 1979 F150 4x4 with the original 148,000 mile 351M engine. I bought it about 3 weeks ago. If you accelerate too fast, it stumbles and hesitates badly. If you take off at a low start, it eases on down the road ok. Once you get up to about 42 mph, you can mash the accelerator to the floor and it will respond with no problems. Before 42 mph, whenever you give too much gas, it hesitates and stumbles until that magic number, then it runs good. Any thoughts or past experiences with a similiar problem? The list of things to check and replace is quite extensive in the troubleshooting guide in my Chilton. A new Engine will be built this fall, so just trying to get it to run a little better until then without investing too much money on it now.Thanks!
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MLariviere Moderator Posts: 2393 From: Biddeford,Me.USA Registered: May 99
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posted 05-25-2002 09:10 PM
It sounds like you need a carb rebuild. It could be the accelerator pump is weak. Another thing to look at is ignition. I had an 85 with a 351W and it did that. It turned out to be the cap. It had some tracking in it and was crossfiring,with the same symptoms you describe.
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skips69 Gearhead Posts: 124 From: Catlin, IL USA Registered: Mar 2001
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posted 05-25-2002 10:24 PM
The cap and rotor would be the first thing I replaced too since it is the easiest and by far the cheapest thing to throw at it. You know how it rolls from there sometimes, so I'll probably start there.
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skips69 Gearhead Posts: 124 From: Catlin, IL USA Registered: Mar 2001
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posted 05-29-2002 09:07 PM
Replaced the cap and rotor finally today. Man, what a big difference. They were pitted pretty bad. Now it runs much better and smoother. Still some hesitation, but only up to about 25 MPH and not nearly as bad getting up to speed. I have aline on a 400 C.I. motor with only 5,000 miles on the rebuild. It is from another 79' truck. I hear the advantages over this motor as opposed to what I currently have (the 351M). What are the basic differences between the two - just cranks and connecting rods? Why is the 400 more popular? And, finally if using this engine, will all my brackets, mounts, etc from the 351M bolt on with no problem? I would think so.Thanks as always!
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1MonsterEffie Journeyman Posts: 6 From: Gloucester, VA Registered: May 2002
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posted 05-29-2002 10:23 PM
Do you still have the stock exhaust? It is strange, but I have heard of trucks that people thought were ignition/carb problems causing hesitation, but in fact it was the catalytic converter clogged up. Being a '79, you will have one unless the exhaust has been replaced, maybe you should look into this.
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skips69 Gearhead Posts: 124 From: Catlin, IL USA Registered: Mar 2001
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posted 05-30-2002 07:30 AM
It may, I'll check that out. It is very quiet, so it could be the original and still have the cat on it - definately single exhaust (for now). Thanks for the tip.
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MLariviere Moderator Posts: 2393 From: Biddeford,Me.USA Registered: May 99
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posted 05-30-2002 09:03 PM
I'm leaning more to a worn out accelerator pump.
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4Zsnow Journeyman Posts: 25 From: Western Washington, USA Registered: May 2002
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posted 05-30-2002 11:57 PM
I second the pump theory.2 pennies ------------------ God Bless Big Oil
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skips69 Gearhead Posts: 124 From: Catlin, IL USA Registered: Mar 2001
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posted 06-02-2002 09:00 PM
Went ahead and finished up the tune up today - New plugs, wires, air cleaner, oil breather and PCV Valve. Runs like a totally different truck now. Very responsive at any speed, great acceleration, etc, etc. The #4 plug was an autolite, all else were champions. That tells me the past maintenance practice for this truck. Either the previous owner or his mechanic intentionally left that plug because of the difficulty in getting to it due to the heater/A-C box being in the way. Everything was badly worn, filthy or pitted on this truck's basic tune up components, so it hadn't been done for quite some time I would imagine. Didn't even check the timing, but that will be next. Just glad to have it performing so much better for now.
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