Author
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Topic: Carb problem
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kid vishus Gearhead Posts: 6220 From: middle of NC Registered: Oct 2000
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posted 07-16-2003 01:45 PM
I don't normally have many problems with carbs, but I appear to have run into a problem with my old gas carb I can't figure out. First of all, it's a 750 DP annular discharge carb with no choke. We (actually dadv) bought it new in '94 I believe and it has never been apart except for jet changes and powervalve changes. It always worked real good, til now.I put it on the KK's motor, and right away it smoked at idle (her dad's backup carb does not do that on this motor so I know it's a carb issue). It was a over rich condition causing it. I changed powervalves in the front (plug in the back), thinking that might be causing it. It wasn't. I pulled it off, and while looking at it I found the vacum cap that was on the big port in the baseplate in back was cracked badly. Thinking it had a bad vacum leak, I replaced it. Didn't help. I decided to change all the vacum caps (one did have a small hole in it). No change. Then I decided to fool with the idle richness screws (4 corner idle). The more I turned them in, the faster it idled. I had all of them originally turned out 1 1/2 turns. Now they are only out 1/2 turn, except for the back one on the passenger side and it;s out a full turn, and I had to lower the idle almost 1000 rpm. And, it appears it has stopped smoking at idle. I figured it must still have a vacum leak, so I took a can of carb cleaner and sprayed all around the base of the carb. No change. The only time the idle changed at all was when I sprayed it directly on the vacum port on the front metering block, then the idle slowed down. I would like to use this carb as I feel it will be faster than her dad's carb (even smoking going down the track it currently is only about .06 slower now), but I am stumped as to what is causing this. Is it possible the gaskets under the 4 corner idle screws have dried out? Any ideas would be greatly appreciated. (edit I have checked both float levels and they are fine. [This message has been edited by kid vishus (edited 07-16-2003).]
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Tbird Gearhead Posts: 298 From: USA Registered: May 2003
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posted 07-16-2003 01:55 PM
If it were a vacuum leak at the base or some other place, when you sprayed carb cleaner around it, the idle/rpm would have went up and the engine would have smoothed out.It sounds more like the idle circuitry is too fat for the signal the carb is receiving. You might try removing the metering plate(s) and inserting a small diameter piece(s) of wire to lean out the idle circuit. Does it have a pcv system hooked up? If not, you might try adding one to give the carb more air underneath the idle transfer slots to lean it out. Not sure about this, but is there a chance someone put the wrong metering plate gaskets on the carb? 2 circuit metering gasket when it needs a 3 circuit or vise versa. [This message has been edited by Tbird (edited 07-16-2003).]
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n2oMike Gearhead Posts: 2499 From: Spencer, WV Registered: Jan 2001
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posted 07-16-2003 02:03 PM
quote: Originally posted by kid vishus: so I took a can of carb cleaner and sprayed all around the base of the carb. No change. The only time the idle changed at all was when I sprayed it directly on the vacum port on the front metering block, then the idle slowed down.
If it's a small leak that is 'sucking air' it can cause a faster idle. Sometimes a spray will close off that leak temporarily and slow the idle speed. You might want to take the whole carb apart and clean it really good... especially if it's been sitting on the shelf for a while. Good Luck! ------------------ Mike Burch 66 mustang real street 302 4-speed 289 heads 10.63 @ 129.3 http://www.geocities.com/carbedstangs/cmml_mburch.html http://www.fortunecity.com/silverstone/healey/367 http://www.mustangworks.com/cgi-bin/moi-display.cgi?220
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kid vishus Gearhead Posts: 6220 From: middle of NC Registered: Oct 2000
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posted 07-16-2003 02:29 PM
Thanks for the replies. If anyone put the wrong metering block gasket on it, it would have been me. DadV might have paid for it, but I did all the tuning on it. The last time we used it, it worked real good. So whatever has went wrong, has happened while it was sitting.I just replaced all the gaskets on the richness screws. Now, it doesn's seem to matter where they are turned except for one of them. And if it's turned in too far it kills the motor. The rest of them don't change a thing. It has been sitting awhile, but it was in a plastic bag in the Holley box. but I suppose it's possible something got in it. All I know for sure is, I will figure it out. But till then, I'm not going anywhere without the McGee backup carb along.
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BlueMule Gearhead Posts: 1494 From: Kent Island, MD USA Registered: Sep 2002
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posted 07-16-2003 02:32 PM
KV... You didn't say what color smoke. We may be sending you off chasing after gremlins that ain't there.------------------ -Paul 70 Mach1 351C 79 Ranchero GT 97 Expedition XLT 5.4 00 SVT f150 Lightning 4149 of 4966 Born on: 06/26/2000 'If you're not the lead dog, the view never changes.'
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kid vishus Gearhead Posts: 6220 From: middle of NC Registered: Oct 2000
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posted 07-16-2003 02:38 PM
It has to be fuel smoke. It smells like an excessively rich problem. The only time it does it is with my carb on it. When I bolt the McGee carb on it, it stops smoking entirely.The first time we tried to use my carb it was so rich at idle it fouled a plug. That was the first time I had ever fouled a plug when running an MSD set up. When I changed the plugs in it that day, they were sooted up badly. No, there isn't a PCV system on it. It does have a pan evac system plumbed into the hedders though.
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BlueMule Gearhead Posts: 1494 From: Kent Island, MD USA Registered: Sep 2002
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posted 07-16-2003 02:57 PM
Eewww... Fouling plugs is nasty. Since it sat for a while, some old fuel may have turned to goo where air is usually supposed to pass. Since it was good when you put it away and now it's crappy, that kinda rules out worn hardware. It has to be goo or a dried out non-metalic component. Since you replaced the soft seats under the mixture screws, I'd take it apart againg and give all the hard parts a dunk in the most vile concoction of parts cleaners you can come up with and then shoot the daylights out of theme with shop air. What do you think? ------------------ -Paul 70 Mach1 351C 79 Ranchero GT 97 Expedition XLT 5.4 00 SVT f150 Lightning 4149 of 4966 Born on: 06/26/2000 'If you're not the lead dog, the view never changes.'
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Dave_C Gearhead Posts: 994 From: Gadsden, Al Registered: Aug 99
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posted 07-16-2003 03:01 PM
On my old door car I ran that carb before I bought a 950HP. The annular boosters are very sensitive to how much vac it's pulling. It doesn't take much to start the main cicuit working. It soemtimes happens if you use one of these carbs on an engine with a cam that pulls good vac.Since the idle screws have no effect it tells me it's running on the main circuit. If it worked fine on another engine I bet the other engine had more cam. Mien had the same problem when it was still a street car and had a milder cam than what I ended up with. The idle mixture screws had zero effect. It was pig rich at idle. You could barely sit in it at idle with the windows down. I cured mine be drilling the throttle blades on the primary side. I had a small hole in each blade. About 3/32" I think. Later, David Cole
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Tbird Gearhead Posts: 298 From: USA Registered: May 2003
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posted 07-16-2003 03:21 PM
Found on a carb tuning siteIf your idle mixture screws do not respond to adjustments, you may have several different problems. The most common is using the wrong carburetor for the application. Smog carbs with reverse mixture screws (these are the ones with the little decals, telling you to turn the screws in for richer mixtures) only have a small band of adjustment built in. Smog carbs work well on stock engines only, and you can't expect them to work well on a modified engine, especially one with a lopey cam. Another common cause of non-responsive idle mixture screws is having too much (more than .040 inch) of the idle transfer circuit exposed. The idle circuit allows a very small amount of finely metered fuel into the engine. By exposing the transfer circuit too much, the gross feed of fuel coming out of the transfer circuit overpowers the fine amount coming out of the idle ports. This is akin to adding a squirt gun's flow into a garden hose's flow...the fine amount of the squirt gun is so insignificant compared to the garden hose, that there is no way that adjusting the flow of the squirt gun will make any difference. There are several ways to fix this problem: 1. If your engine is worn, or has a big vacuum leak, you should fix those problems before trying to crutch your carb. Sometimes, with worn engines or one with a vacuum leak, the carb must be opened quite a bit just to get the engine to run. 2. Buy the right sized carb! If you're trying to use a 600 cfm carb on a lopey-cammed 460, then you must open the primaries too far into the transfer slots just to get enough air into the engine to get it to idle. A larger carb on this example would have a larger throttle plate, which would need to opened less to allow the engine to idle. 3. Open the secondaries a bit, and close the primaries a like amount. This will allow more air in, without exposing quite so much of either primary or secondary transfer slots. 4. If opening the secondaries doesn't work, then you may have to drill small holes (1 per plate) in the primary throttle plates to allow air in while the plates cover the transfer slots. This is a trial and error procedure, so start small, about 1/16 inch. You should not have to go much larger than 3/16 inch. Drill on the side opposite of the transfer slots, to help keep this added airflow away from the idle ports and transfer slots. Maybe this will help some.... or this picture from holley.... Bigger pic here http://www.holley.com/HiOctn/TechServ/TechInfo/TI-219.html
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kid vishus Gearhead Posts: 6220 From: middle of NC Registered: Oct 2000
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posted 07-16-2003 04:38 PM
Since it doesn't act this way with the other carb, I can basically rule out a vacum leak (unless it's the carb itself.) If it doesn't rain tonight we are taking it to Test N Tune. If it acts "ugly" on the first pass, I will swap carbs.I'm starting to think it needs the secondary blades opened up a bit as it is probably running on the main circuitry at idle. Thanks everyone. I will let everyone know what I find (or how it runs tonight).
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Fordwiser Gearhead Posts: 408 From: Metamora, Illinois Registered: Dec 2000
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posted 07-16-2003 06:44 PM
First thing I would try is shoot some carb cleaner down the air bleeds let it set a few minutes, then blow them out with compressed air. Roger
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kid vishus Gearhead Posts: 6220 From: middle of NC Registered: Oct 2000
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posted 07-16-2003 07:49 PM
quote: Originally posted by Fordwiser: First thing I would try is shoot some carb cleaner down the air bleeds let it set a few minutes, then blow them out with compressed air. Roger
That was one of the first things I did do. It didn't help at all. Since it decided to rain tonight, we'll have to wait till saturday to give it a try. Maybe I'll crack the secondaries open a bit first now that I have a couple of days before we go.
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Buster Gearhead Posts: 1466 From: Hurricane alley Registered: May 2002
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posted 07-16-2003 10:50 PM
quote: Originally posted by Fordwiser: First thing I would try is shoot some carb cleaner down the air bleeds let it set a few minutes, then blow them out with compressed air. Roger
That sure sounds like it... might take the metering block(s) off while you do this, just to make sure your getting a clean shot through the air bleeds. btw, what size engine is this? The annular boosters are very sensitive to how much vac it's pulling and lg CID engines. [This message has been edited by Buster (edited 07-16-2003).]
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jsracingbbf Gearhead Posts: 2805 From: Batesville,MS. , U.S.A. Registered: Mar 2002
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posted 07-16-2003 11:46 PM
I ain't no carb man but I think your onto something KV, I think the back blades need to be cracked open a little more. Not enough air at idle. Or do what Dave C said. I always try the back adjustment screw before I drill the butterfies. It's worth a try.
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kid vishus Gearhead Posts: 6220 From: middle of NC Registered: Oct 2000
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posted 07-17-2003 07:46 AM
It's a 357 inch windsor. So it's not like it's a really large motor.
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Moneymaker Administrator Posts: 26513 From: Lyons, IL, USA Registered: May 99
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posted 07-17-2003 10:19 AM
Try cleaning out the Air bleeds.------------------ Alex Denysenko Co-Administrator and Moderator NHRA/IHRA/SRA member and licensed Superstock driver MCA member# 53321 NHRA and IHRA SS/LA National Record Holder '00,'01,'02,&'03 First SS/MA in the TENS! Fleet of FoMoCo products including 88 ASC McLaren Mustang #28 Professional Manwhore The Barry of BarrysGrrl Quote #1: "I never met a magazine mechanic I liked." Quote #2: "Make sure brain is in gear before engaging mouth!" Quote #3: "If you can't run with the big dogs, stay on the porch!" www.moneymakerracing.com
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bluestreek Gearhead Posts: 1724 From: Athens,GA Registered: Jul 2001
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posted 07-17-2003 09:01 PM
Did you replace the bowl and block gaskets? Hard gaskets can cause fuel leaks between the circuits in the block and lead to a rich condition.My 750 HP was blowing soot at the track once and I found out that the primary bowl was dumping fuel into the boosters under a hard pull. Turned out to be a problem with the float assy. I added new needle & seat and changed primary float and the problem was instantly cured. How much vacuum does it have at idle? A 1/2 to 1 turn on the mixture screws is not that unusual for a 750 performance carb on a mild SBF. It depends on the idle rpms and amount of vacuum it pulls at idle. My 331 has about 12.5" at 900 rpms and it only uses about 3/4 turn on all 4 corners on the street. At the track I richen the idle mixture up about 1/4 turn more for better reaction with the stick shift. Hope you figure it out. Let us know. Good luck at the races! ------------------ 1966 Mustang Coupe: Custom glass hood and BIG scoop sits atop a 289 stroked to 331 c.i., Steel crank and girdle, 5.4 H-beams, Forged slugs, TFS alum. heads, ported Stealth 8020 intake, Xtreme 274 Solid Roller, Holley 750 HP, long tubes, 4speed, 9" 3.50 posi. 11.86 @ 116 mph (7.62 @ 93 mph)full street trim! DanH
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kid vishus Gearhead Posts: 6220 From: middle of NC Registered: Oct 2000
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posted 07-20-2003 10:20 AM
We did get to go racing last night. We made the first pass with the 750 annular carb since it wasn't smoking at idle anymore. Her first pass with it was a touch slower than what the car ran last week (8.09 as opposed to 8.06) and the mph was down about 1 full mph (85.6 as opposed to 86.4). Knowing it was slower than last week with her dad's carb, and the since she was only getting 2 time runs, we decided to put her dad's carb back on to try it. It was .02 slower than my carb but the mph was better. It appears as if my carb is working "right" now. But we really need to get to a test n tune so she can make several passes with each carb and then we can compare times. I think I'll fatten my carb up a tad before we go again. Thanks to all.
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Strain Gang Gearhead Posts: 220 From: Thor, Iowa Registered: Mar 2003
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posted 07-20-2003 10:46 AM
Hey Kid, I have been fighting carb problems all year as well. The thing loads up at idle, but runs good down the track, I have to have the front throttle plates open a long way so the car dont die when Tom puts it in gear, and when I try to set the 4 corner screws, the back does not respond to change at all. I'll be straight up with you, I dont know jack about Carbs, except for jetting and the obvious. But when it come to diagnosis....STUPID! Than a friend came over to check it out for us and found the little screw that holds the Sec. plates open a touch fell out and was completely closed off. Ran the car the rest of the night, got home and had Tom start the car and let it try to idle. Took a small screwdriver and cracked the Sec. plates open a touch, and WHALLA the idle picked up and car idled smoother than ever. All the headaches for a .50 cent damn screw. Just wanted to share. Steve.
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